Hello, i have heard that during the sinking one of Titanic's main bulkheads failed and collapsed, causing the compartment to be flooded and the ship to sink further, did this actually happen and is there any proof of it?
Also, if you wondering, i'm doing ok when it comes to COVID-19, lockdown and all that, i haven't come down with a cold yet and i hope i never
Oh wow...I thought this issue was pretty much put to bed!?! There is absolutely
NO WAY that
Watertight Bulkhead E (separating Boiler Rooms 6 & 5) collapsed during the sinking process. Of course we're talking about lead fireman Fred Barrett's testimony of a massive surge of water emanating from the forward starboard end of Boiler Room 5 at approximately 1:15 AM or there about. Without question the massive deluge of water that Barrett described in his testimony was the result of the aforementioned Coal Bunker's hatch doors (which weren't designed to be watertight) giving way to a sudden, explosive surge of water which had accumulated inside the bunker (
Coal Bunker W if you want to get precise and in line with H&W's schematics) filling the mostly empty bunker (most of its coal had been removed earlier to unseat a coal fire) with sea water as a result of damage caused by the 11:40 PM collision or allision with the iceberg.
For about an hour and a half Coal Bunker W in Boiler Room 5 had been steadily filling with water until the pressure from all that seawater was too much for its vertical sliding hatch doors to withstand and it or they gave way producing a violent rush of water which was apparently convincing enough to cause Engineer Herbert Harvey and Lead Fireman Fred Barrett to abandon the Boiler Room and the task they had been working involving the compartment's pumps.
During the American inquiry the idea developed based on Barrett's testimony of the 1:15 AM onrush of water that it was very likely caused by the failure of Bulkhead E allowing water into Boiler Room 5 from a very
FULL Boiler Room 6 that was the issue. However when one examines the known facts and quantities at play that night it becomes clear that there was no catastrophic failure of the bulkhead in question which would probably would have resulted in Barrett's death. What's more, the coal bunker fire that's often cited as the culprit for this false event in no way significantly compromised the structural integrity of the subject bulkhead. Titanic's bulkheads and the hull's shell plating was made of
mild steel. This is a type of steel with a
VERY LOW carbon content. It is the presence of carbon in steel alloys that can cause steel to become brittle if exposed to red or white hot temperatures without benefit of undergoing special heat treatment (which actually makes steel much stronger). Mild steel's low carbon content means it can be repeatedly exposed to very high temperatures (caused from say, a coal bunker fire) and
not become
brittled when it returns to normal temperatures (either by quenching with water or being allowed to cool down on its own.)
I hope this and the illustration I drew up and attached below might help others to better conceptualize what occurred with respect to Coal Bunker W of Boiler Room 5.
Sincerely,
Robert House
BELOW:
Coal Bunker W of Boiler Room 5 fills with water through an approximate 2 foot long damaged section Titanic's shell plating. The ship sustained a series of partially open seams in the hull's shell plates which actually came to an end at the location of the subject bunker. Coal Bunker W prevented flooding from entering the main area of Boiler Room 5 although curiously there appears to have been no attempt early on to use the Boiler Room's pumps which had the capacity to handle the rate of ingress inside the bunker with room to spare. With no apparent scuppers built into the floor of these coal bunkers the only way the coal bunker's flooding could have been removed was to let the room to fill to the bunker's hatch door(s) allowing it to crest over the threshold and into the main working space where it would find its way below the stokehold plate flooring and into the centrally located scupper drains where it would be removed. Needless to say this would have done very little to slow the sinking process that night...but it was an option available to the crew which wasn't taken.